KLX recently tackled one of the most challenging emerging technologies, a split-string, coiled tubing well intervention, by rethinking how dual-string work is executed. After extensive research into the root causes of common issues, our teams redesigned the process...
Challenges Well had potentialcommunication issues withother wells in the area Solution Utilize KLX HC CompositeBridge Plug to isolate eachstage to ensure proper zonetargeting and reducecommunication with othercompleted zones. Results All 26 plugs set properly...
LOCATION: Denver-Julesburg Basin (DJ) CASING SIZE: 5-1/2″ 20# (Casing ID 4.778″) BOTTOM HOLE TEMPERATURE: 189 degrees F FLUID TYPE: Reclaimed Produced Fluid # OF PLUGS INSTALLED: 83 MAX PLUG SET DEPTH: 11,871 feet MAX LINE SPEED: 499 feet per minute MAX...
Challenges Well had previous casing damage. Casing Patch at 4000 ft, located above KOP. Solution Utilize KLX HC Composite Bridge Plug to isolate each stage to ensure proper zone targeting. The KLX HC Composite Bridge Plug also has a narrow OD that allows a seamless...
One Hour Frac Plug Dissolution A 15% hydrochloric acid solution and a 50°F test temperature enabled the new KLX Dissolvable Frac plug to achieve practically complete dissolution in just 60 minutes. Test Conditions KLX customers like to be ready for anything, and this...